The demolition and removal of the old generator started early Sunday morning. Mark headed into the engine compartment with a hack saw, large wrench, big hammer and lots of determination. At first parts were coming off fairly easily (as easy as can be expected with a 40 year old machine that has lived in a salty environment for most of those years!). I moved these smaller parts onto the pier to get them out of the way.
By 10am, it was time to tackle the main generator body, weighing in at about 400 lb. Our friend Steve came to join in the fun and together with Mark, they came up with a plan. We had lots of left over carpet from our main cabin so Steve came up with the idea of wrapping the generator up like a burrito and then sliding/rolling it out of the engine compartment. The first challenge was getting the generator passed the main engine – no easy feat! The 2 men lifted the greasy, dirty generator on top of the engine and rolled it out into the passage way. After that it was relatively easy to slide/push the generator out of the passageway and up to the base of the ladder.
The next step required a whole lot of discussion – how to get this 400 lb piece of dirty metal up and into the cockpit (about a 5 foot lift) with just 2 guys. There was talk of finding 2 more guys to help dead lift it but that seemed risky (my back hurt just thinking about that scenario). In the end it was decided to use our chain hoist to lift it out. At this point, we stopped for lunch and then went on the hunt for some blocks of wood and a 4 x 4 piece of wood that the hoist could be secured to.
Okay it’s time to lift this sucker out of the boat. Slowly it rose off the floor and headed towards the companionway opening. As it reached the top, it became obvious that the hoist itself was stopping the generator from getting to a good height to be pushed into the cockpit. Down it went, back to the floor!! Round 2 – I suggested turning the generator on it’s side (it’s taller then it is wide), so the hoist hook was moved to the side. Up it went again – Steve was cranking on the hoist and Mark was guiding it up. This time it made it high enough to get into the cockpit but when Mark and Steve started to maneuver it towards the opening, it got jammed on both sides.
This was when all hell broke lose!!! I ran over to help Mark push while Steve pulled and twisted the generator to get it unstuck. As we were doing this, the wood and chain hoist holding our 400 lb piece of metal fell aside and we were left with a generator wedged in the companionway opening. No panicking allowed at this point (that’s what I said in my head). Quickly Mark tossed the rope securing the carpet around the generator to Steve and Steve tied it around the binnacle. Once the generator was secured, Steve gave it one good twist and it slid into the cockpit. There were a few minutes of stunned reactions and then some major celebrating. We got it into the cockpit and no one got hurt (and we can use the boat again!😁)
Once the generator was in the cockpit, it was a little easier to move around and after a bit more pushing, sliding etc, the generator was on the wooden dock beside our boat. Now it had to be lifted another 5ft or so to get it onto the pier. With the help of 2 more men and our car, the generator found a new home on the pier and our boat lost about 500 lbs of weight.
At the end of the day, we headed over to Jane and Steve’s boat for happy hour which turned into an awesome dinner!! It was a great, tiring day followed by a great evening. Monday was definitely a low key kind of day!!

















































































